Category Archives: Restoration and Repair

Electronics restoration projects.

Restoring HP 403B AC Voltmeter (10Hz – 2MHz)


The following instructions, document the process that I toke to restore the  HP 403B AC Voltmeter to working order.

Day 1

The unit was a bit dirty when USPS delivered it to my front door. The rechargeable battery pack is showing sign of corrosion.

First, I checked the meter movement and making sure that it is in good shape.

The moment is smooth and doesn’t appear to have any issue. With a 1.5V battery and a variable resistor, I checked the full-scale reading and a few other reading just to confirm the meter linearity.

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A quick check of the voltage across the capacitor C21 and I am getting a steady 42.28V DC.

Next, I checked the battery +13, -6 and -13 supply voltage. I am getting +10, -6.5 and -13, this is because the battery is so old and some of the cell are dead and not evenly charged.

Even though the supply voltage are way off! The good sign is that the unit is fully working.

The battery is showing sign of corrosion and need to be replaced. So, it’s on my next to do list.

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After a quick search, I found suitable replacement battery from eBay. The seller is trying to get rid of his inventory and selling a 25 packs of 3.6V 700mAh for cordless phone for only $0.99. The only catch is the $20.00 shipping.

The meter originally came with 4 x 6.0V 225mAh Nickel-Cadmium Battery but I am going to replace it with 8 x 3.6V 700mAh battery packs made for cordless phone.

The combined voltage will be slightly higher when it is fully charged, however, it doesn’t seem to pose any problem after everything is re-calibrated.

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After tying them together and solder their leads in series connection to make 2 x 14.4V batteries pack.

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I reconnect and the battery to the original +13, -6 and -13 leads and put everything back together.

NOTE:  Don’t solder the -13 lead just yet, as you will insert the amp-meter in series with it to adjust the charge rate later on.

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I made some minor change to the orientation of these batteries after soldering them in place, so that the PCB will fit on top.

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With the Amp meter connected in series with -13 power line, I adjust the pot to 6.5mA as suggested by  the manufacturer. You may set it to 11mA, if you plan to use it on battery regularly.

I let it fully re-charge over night before I return to work on it again.

Day 2

As I am going over the calibration procedures.

I notice that when meter is on, it never quite return to zero. It is alway 2 ticks higher.  Which kinda annoy me.

TODO: Investigate to find out which aging components causing this.

But for now, I just re-zero it with the zero adjustment screw. This will affect it accuracy a little bit. However, when checking the voltage indication on each range the reading track very closely to my HP 334A reading. So, for now it is not an issue for me at the moment.

The strange thing is that, on these HP AC Voltmeter. There is only mechanical zero adjustment. Unlike most VTVM that I had restored. Where you have to adjust  mechanical zero, AC and DC zero.

Day 3

While calibrating, I notice that on 0.01 and 0.03 range. The meter doesn’t work at all and it’s alway peaking.

It seem the meter is fully deflected when those range are selected.

At first, I though some resistors in the voltage divider network are bad. But after checking these resistors, switches and signal path. Everything checked out ok.

So, to diagnose this further. I connected the oscilloscope to take a peek at the signal at each stages.

After tracing the signal path on the diagram, the original input signal is amplified and then going into the resistor divisor network.

When I connecting the probe and observe the output at R20 and R22, There is 11mV p-p (.048us or 21MHz) voltage showing  on the scope.

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In the 0.01 and 0.03 range, the original signal coming out of the voltage divider  is so small compare that with the 11mV p-p noise.

The noise is swamping the original signal and causing significant meter reading error.

NOTE: According to the manufacturer manual, this may be caused by a noisy transistor and need replacing.

But first, I wanted to try to fix it by adding a filtering capacitors.

After adding a 0.1uF 50V to +13V and -13V to ground, this seem to eliminate the noise.

To install the capacitors, I find some open space on the PC board and solder them in place.

This help to remove the noise and making 0.01 and 0.03 range working again.

IMG_9808As seen below the signal is much cleaner now.

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Day 4

Spend a few hours calibrating the meter the best I can. Due to lack of a signal generator that can put out 30V 300kHz sine wave, I have to put off those calibration steps.

At the moment, the meter is track accurately from 1mV to 1V from 10Hz – 2MHz.

TODO:

  • Recap
  • Finish up calibration at 300kHz

 

Link to Service Manual:

Click to access HP-403B-Manual-SNprefix-403.pdf

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Restoring Heahkit IT-17 Tube Tester


I acquired quite a bit of old test equipments lately and some of them are based on old vacuum tubes. Most of the time during the restoration process, I am able to get them working without the need of the tube tester. So, a tube tester is on my wish list but it’s not a high priority.

Out of a blue, I stumbled up on a Craigslist listing of 10+ test equipments at really good deal. The piece that I am really interested in buying was the Heathkit IT-17, the rest are nice too but I have no use for them at the moment.

The seller listed it pretty early in the morning, so the chance of it still available when I saw the ad was pretty slim. So, I decided contacted him late in the night anyway.

Early next morning, I got a response back and they are still available. I was so elated when I heard the news. I immediately arranged the time to drop by and drove 50+ miles to Oxnard to pick them up. While I was there he also offered to sell me a box of tubes at really good price.

The Heathkit IT-17

The unit was really an ugly duckling and disgustingly dirty when I pull it out of the box. The back cover is dirty and the paint are peeling. The good thing is that the front panel is still in pretty good shape.

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Restoring

With the case opened, I quickly examined all the soldering join and looking for burned components. Everything looks good. I went ahead and replaced all bad carbon resistors that are out of tolerance and cleaned all switches and pots with contact cleaner.

I initially followed the IT-3117 instructions, since I can’t find the original IT-17 manual anywhere on the Internet. The only thing I found was the IT-17 schematic and the two are quite similar in design. I proceeded to check the continuity from the switch to all the pins on each socket, they are all good. The filament voltage, however, it is really off and the line test is off-center but the unit is functional.

Testing

With the tube tester semi functional, I decided to give it a test run. With a box of unknown condition tubes at hand, I tried to test some of them. After going through 1/4 tubes in the box I got 2/3 of the tubes are bad and 1/3 are good.

With 2/3 bad tubes start piling up, I started to question the tube tester functionality because who would keep a bunches of bad tubes???

Manual Testing

I decided to do manual testing on 6L6 which was tested bad earlier.

  1. Connected pin 2 and 7 to external power supply the filament is glowing nicely at 6.3 DC. So, the filament is fine.
  2. When connected to the socket on the test tube. The filament is not glowing at all, 0V is measured between 2 and 7.
  3. When 6L6 is not installed, there is 6.3V between pin 2 and 7.
  4. I decided to plug 6L6 tube back in and use the alligator jumper wire and connect pin 2 and 7 to corresponding wire on the switch bank. The filament start glowing nicely. This confirm the socket is making clean contact, but the wiring is possibly bad.
  5. Measuring the resistant from the switch to pin 2, the wire has 50+ Ohm?? Note to self – Don’t trust the continuity beep!!!
  6. After some tracing, it appears that the original builder missed one solder join on one of socket. After fixing that the 6L6 filament start glowing again and the tube tested fine now.

Calibrating Tube Tester

All original instructions assumed that all parts are new and working to spec. So, some of these assumptions are no longer valid since the meter is old and not that accurate. This is true at least in my case, when the meter is zeroed, the reading are way off.

I have to come up with alternative way of calibrating it and ensuring that the tube tester result are some what usable.

Calibrating Line Test Indicator

  1. With no tube in any of the socket
  2. Set all switch to center position, then set A to bottom
  3. Set the filament to 110
  4. Connect a voltmeter black lead on pin 1 and connect red lead on any other pin so we can read the filament voltage. This is important, since the during line voltage adjustment, the meter is connected to 110V tap on the filament winding. At 110V the meter should be reading 50 or .5mA. If not check the 1K and 75K resistor and make sure they are within tolerance.
  5. Turn set line until the filament voltage reading is 110V RMS. Cut a piece of electrical tape in triangle shape and tape it to set line dial to mark this position. This is the correct line voltage for use with the tube tester.
  6. When set line voltage is properly adjusted, the filament voltage reading should be 110V. At this point the meter should be reading exactly 50 or .5mA. This is assuming that the 1K, 75K and your meter are good. If 1K and 75K are good but the meter is not at 50, the meter reading is off. In that case,insert an amp meter in series with the panel meter to get the correct reading, it should be around .5mA. Then adjust the panel meter so that it’s indicating the same reading by turning the zero adjust screw on the panel meter. Once that is done, your set line switch and meter is properly calibrated to show proper line voltage. NOTE don’t adjust the mechanical zero from now on it will screw up the reading.
  7. Next insert a known good tube and set the tube tester accordingly. Then the plate control is adjusted so that the meter is reading from 0 to 100, the measured value from amp meter still inserted in series with the panel meter is recorded at each point to produce a table and chart.
  8. From now on, after testing using the original instructions. Take the reading and use the table to map it to actual value in mA or multiply that by 100 to get % scale.

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Restoring ESI 250DA Impedance Bridge


Recently, my wife and I started attending the swap meet at TRW parking lot in El Segundo California regularly on every last Saturday of the month. This is one of the things that we enjoy doing in the morning before we heading to Hong Long restaurant.

On this particular morning we spotted an ESI-250DA impedance bridge made in the 60’s from one of the vendor. I decided to make inquiry of the price and he was asking $20 for it, but the item has rust from water damage and missing the null indicator tube.  I was not willing to pay so much for it, so I made a final offer of $10 for the thing in part trying to give him some business. He agreed and now I am a proud owner of 1960 old relic.

Normally I don’t buy stuff in such a sad condition. However I hate seeing useful instrument going to the land fill and also this will keep my mind busy for awhile.

Day 1

I brought the unit home and open it up. The top part of the interior are okay, luckily no rust there. The bottom section however has large amount rust deposited at the bottom. Luckily the key components like standard capacitor, resistors and switches are in decent condition.

The first priority is to remove the rust on the transformer and the chassis. I didn’t bother to remove the rust on the case until the very end.

Day 2

Cleaned all the contacts and switches with contact cleaner and oiled the switches.

Day 3

Inspected all the capacitors and they are all bad and need to be replaced.

I went a head and replaced with all electrolytic capacitors with near equivalent, since exact replacement is impossible to find. As long as they are still within the original specified tolerance it should be okay.

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Day 4

There were a huge amount of white stuff deposited on the Selenium Diodes. So, I decided to replace them with Silicon diodes instead since, they are so old will fail anytime now.

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Turned the unit on and the 150 Ohm resistor in the power supply section started smoking. I quickly turned it off but the damage was done.

Day 5

Replaced the 150 Ohms with 390 Ohm 5W and replaced 2.2K with 2.2K 5W resistor as shown below. When replacing selenium diode with a silicon diode, it is commonly recommended to use 300 Ohms or more in series with silicon diode to limit the surge current.

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Turn the unit on and everything seem to be okay and the tubes filament start glowing amber. 🙂

Attempted to measure some resistors, however the needle would not budge.

Day 6

Dissembled the galvanometer to take a look inside. The meter resistant tested fine, however the needle was frozen solid.

Wasted 1/2 hours tapping the tube to loosen the rusted innards. Finally got the pieces separated, the interior were badly rusted and huge amount of  metallic dust stuck on the magnet.

I carefully disassembled the magnet and gently clean up the coil and removed as much rust as I can. As seen below some rust still remain, I don’t want to clean it up too much since it’s very delicate and held together in place by a thin wires.

Finally sprayed some WD-40 on the part to remove any remaining rust.

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Here is the galvanometer cleaned and reassembled.

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I reinstall the galvanometer and did some resistance measurement and the null meter seemed to work now.

Day 7

Did another series of checks to confirm the standard resistors and capacitors. All checked out okay and very close to specified values.

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Once the above check was completed, I wanted to confirm the accuracy of Rx1 and Rx10 measurement. Did another series of resistance measurement, all are very close to what I am getting from a digital multimeter.

At this stage I have to stop working on it, since I can’t test inductor or capacitor with it because the 6U5 null indicator tube was missing. I found some used replacement tube but they are quite expensive on eBay.

More treasure hunting…

Day 8

Must be my lucky day, I found a 6E5 tube and another magic eye tube with no marking on it. The 6E5 tube that I got, it has bulging shape so it won’t fit into ESI-250DA.

After some Googling the unmarked tube could be a 6U5 or 6E5, which will fit it is a straight tube nicely. Since both tubes specs are quite similar, I guess it won’t hurt just to try it out. After some cleaning, I inserted the tube and turn on the unit. The magic eye start producing a nice green glow. Kinda exciting watching it actually.

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Did another series of capacitance and inductance measurement and every thing seem near the ball park.

Day 9

Spend the morning adjusting the rheostats on D-Q dials to what specified in the service manual.

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Day 10

A fully function unit

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Misc photos

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